really weird behavior. the throttle range calibration on the esc did not work. have tried different things on the hardware side with the esc. nothing works.
To me it "seems" to be some kind of throttle out of range issue. When running the calibration on the esc with my joystick. I can see on the leds, that the esc doesnt pick up the signals on full reverse or full forward. Got to take the stick back 2 millimeters to make it arm. Both ways.
im using a 35A HD esc for cars (with reverse)
mystery D2836 brushless 1700kv
But im pretty shure now that this is a firmware/software issue.
Running the 4-axis joysticksystem (http://principialabs.com/arduino-python-4-axis-servo-control/
Im using the xbox360 controller (but same happen with other controller)
I have read somewhere that the operating range for escs are 45-135?
Right now im running the servo.h with this http://principialabs.com/wp-content/uploads/MultipleSerialServoControl.pde
im not having this issue with servos on the same setup.